Report of the PRESIDENTIAL COMMISSION
on the Space Shuttle Challenger Accident
Volume 5 Index
Hearings of the Presidential
Commission on the Space Shuttle Challenger Accident: February 26,
1986 to May 2, 1986.
MARCH 7, 1986 SESSION (part 2 of
2)
[1237] [Ref. 3/7-93]
Space Shuttle Main Engine: Inspection of Recovered hardware.
SPACE SHUTTLE MAIN ENGINE
INSPECTION OF RECOVERED HARDWARE
- ALL ENGINES RECOVERED IN CLOSE PROXIMITY
TO EACH OTHER AND GIMBAL BEARINGS FAILED IN AN OVERLOAD
MODE
- ENGINES WERE ATTACHED TO THRUST
STRUCTURE AND BULKHEAD AT WATER IMPACT
- ALL FRACTURES WERE DUE TO DUCTILE
OVERLOADS
- ENGINES DID NOT EXPLODE
- DAMAGE WAS DUE TO WATER IMPACT AND
POSSIBLY IMPACT WITH OTHER STRUCTURE
- NO TURBINE BLADE SEPARATION CAUSING
HOUSING DAMAGE
- ALL ENGINES HAD BURN-THROUGH DAMAGE IN HOT
GAS REGIONS DUE TO INTERNAL OVERTEMPERATURE
- TYPICAL OF LOX RICH CONDITIONS DUE TO
FUEL AND LOX DEPLETION
Back